化工学报 ›› 2014, Vol. 65 ›› Issue (6): 2335-2343.DOI: 10.3969/j.issn.0438-1157.2014.06.052

• 能源和环境工程 • 上一篇    下一篇

炭砂双层滤料浮滤池工艺处理藻污染水库水的试验研究

王永磊1,2, 李军1, 张克峰2, 贾瑞宝3, 李梅2, 宋武昌3, 李莹2   

  1. 1. 北京工业大学建筑工程学院, 北京市水质科学与水环境恢复工程重点实验室, 北京 100124;
    2. 山东建筑大学市政与环境工程学院, 山东 济南 250101;
    3. 济南市供排水监测中心, 山东 济南 250100
  • 收稿日期:2013-09-29 修回日期:2013-11-20 出版日期:2014-06-05 发布日期:2014-06-05
  • 通讯作者: 李军,张克峰
  • 作者简介:王永磊(1977- ),男,副教授
  • 基金资助:

    国家水体污染控制与治理科技重大专项(2012ZX07404-003-006);国家自然科学基金项目(51078008);住建部科技计划项目(2012-K7-8);北京市教委重点基金项目(KZ201110005008);北京市自然科学基金项目(8122005);北京市科技创新平台项目(004000546612010)。

Experimental research on treating reservoir water contaminated by algae using GAC-sand dual media filter flofilter

WANG Yonglei1,2, LI Jun1, ZHANG Kefeng2, JIA Ruibao3, LI Mei2, SONG Wuchang3, LI Ying2   

  1. 1. Key Laboratory of Beijing for Water Quality Science and Water Environment Recovery Engineering, College of Architecture and Civil Engineering, Beijing University of Technology, Beijing 100124, China;
    2. College of Environmental and Municipal Engineering, Shandong Jianzhu University, Jinan 250101, Shandong, China;
    3. Jinan Water and Wastewater Monitoring Center, Jinan 250100, Shandong, China
  • Received:2013-09-29 Revised:2013-11-20 Online:2014-06-05 Published:2014-06-05
  • Supported by:

    supported by the National Natural Science Foundation of China(51078008) and the Natural Science Foundation of Beijing (8122005).

摘要: 目前水库水源藻污染日益严重,传统沉淀固液分离工艺难以满足净水要求。以鹊山引黄水库高藻原水为研究对象,开发了炭砂双层滤料浮滤池,考察了浮滤池工艺运行特性及运行效果。试验表明,絮凝剂选用聚合氯化铝铁(PAFC),在投药量4.0 mg·L-1(以Al3+计),回流比8%,溶气压力0.4 MPa时,运行效果较优。炭层所含生物量约占滤料层总生物量的97.4%(最高值50.2 nmol P·g-1),是砂滤层 (3.0 nmol P·g-1)的16.7倍,污染物的去除主要发生在活性炭层。试验期间,浮滤池工艺对颗粒物、蓝绿藻、浊度、CODMn、NPOC、UV254、氨氮的去除率分别达到96.48%、92.40%、92.56%、57.41%、51.60%、52.50%、75.67%,嗅味由4级降为0级,出水土臭素、二甲基异冰片含量均小于检出限,一氯二溴甲烷、三氯甲烷前体物的去除率分别达到55.1%和60%,表明浮滤池工艺对常规指标、藻类、嗅味物质、消毒副产物前体物去除效果显著。

关键词: 藻, 污染, 浮滤池, 浮选, 过滤, 炭砂滤料, 嗅味物质, 消毒副产物前体物

Abstract: The algae pollution of reservoir water is serious increasingly, the traditional process of sedimentation solid-liquid separation hardly meets the requirement of clearwater. GAC-sand-double-filtration flofilter was built to treat the high algae reservoir water derived from yellow river, and the running and operating characteristics of this flofilter were investigated. The experiment results showed that, the effect of running was excellent when polyaluminum ferric chloride(PAFC) dosage was 4.0 mg·L-1 (Al3+), air pressure 0.4 MPa, and reflux ratio 8%. Biomass of GAC and sand filter layer mainly existed in the carbon layer, which accounted for 97.4% (the highest value was 50.2 nmol P·g-1), and its biomass was 16.7 times of sand layer (3.0 nmol P·g-1), so the removal of pollutants occured mainly in the carbon layer. During the test, removal efficiency of particulate matter, blue-green algae, turbidity, CODMn, NPOC, UV254, ammonia nitrogen reached 96.48%, 92.40%, 92.56%, 57.41%, 51.60%, 52.50%, 75.67% respectively. Odor reduced from 4 to 0. Contents of geosmin and methylisoborneol were both less than the detection limit. Removal efficiency of chloroform, chlorodibromomethane reached 60% and 55.1%. The results showed that, flofilter process had a great removal on conventional index,algae,odor substances and disinfection byproducts precursors.

Key words: algae, pollution, flofilter, flotation, filtration, double-layer filtration, odor substances, precursors products of disinfection

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