化工学报 ›› 2021, Vol. 72 ›› Issue (5): 2586-2595.DOI: 10.11949/0438-1157.20201304
谢昭明1,2(),陈庚1,2,刘仁龙1,2,刘作华1,2,岑少斗1,2,陶长元1,2,郭胜惠3
收稿日期:
2020-09-11
修回日期:
2020-10-29
出版日期:
2021-05-05
发布日期:
2021-05-05
通讯作者:
谢昭明
作者简介:
谢昭明(1973—),男,博士,副教授,基金资助:
XIE Zhaoming1,2(),CHEN Geng1,2,LIU Renlong1,2,LIU Zuohua1,2,CEN Shaodou1,2,TAO Changyuan1,2,GUO Shenghui3
Received:
2020-09-11
Revised:
2020-10-29
Online:
2021-05-05
Published:
2021-05-05
Contact:
XIE Zhaoming
摘要:
在软锰矿湿法浸出过程中,采用传统搅拌桨反应器,容易出现流体“打旋”现象,导致传质效果差,进而降低反应效率。因而,本研究将刚柔组合桨应用于软锰矿的还原浸出过程,强化浸出过程的传质行为,提高锰矿浸出率。结果表明,在黄铁矿与软锰矿质量比为0.20,硫酸浓度为1.5 mol/L,液固比为10,温度为363 K下,软锰矿中锰的浸出率达到90.12%,与传统桨叶相比,锰浸出率提高5.5%。同时,研究发现浸出过程遵循核收缩模型且受表面化学反应控制,黄铁矿与软锰矿质量比、初始硫酸浓度、液固比的反应级数分别为1.2679、0.4182、1.1959,反应动力学方程为1- (1-X)1/3=0.96×103(
中图分类号:
谢昭明, 陈庚, 刘仁龙, 刘作华, 岑少斗, 陶长元, 郭胜惠. 刚柔组合桨强化软锰矿浸出过程的反应动力学特性[J]. 化工学报, 2021, 72(5): 2586-2595.
XIE Zhaoming, CHEN Geng, LIU Renlong, LIU Zuohua, CEN Shaodou, TAO Changyuan, GUO Shenghui. Reaction kinetics characteristics of pyrolusite leaching process enhanced by rigid-flexible combined impeller[J]. CIESC Journal, 2021, 72(5): 2586-2595.
O | Mn | Fe | Si | Ca | Al | 其他 |
---|---|---|---|---|---|---|
33.11% | 31.63% | 26.02% | 3.69% | 0.52% | 3.05% | 1.98% |
表1 软锰矿的主要化学成分分析(质量分数)
Table 1 Main chemical composition of pyrolusite by XRF analysis
O | Mn | Fe | Si | Ca | Al | 其他 |
---|---|---|---|---|---|---|
33.11% | 31.63% | 26.02% | 3.69% | 0.52% | 3.05% | 1.98% |
Fe | S | Si | Zn | Al | Ca | 其他 |
---|---|---|---|---|---|---|
50.29% | 38.06% | 2.04% | 5.47% | 1.13% | 1.67% | 1.34% |
表2 黄铁矿的主要化学成分分析(质量分数)
Table 2 Main chemical composition of pyrite by XRF analysis
Fe | S | Si | Zn | Al | Ca | 其他 |
---|---|---|---|---|---|---|
50.29% | 38.06% | 2.04% | 5.47% | 1.13% | 1.67% | 1.34% |
温度/K | 液膜扩散控制 | 产物脱落扩散控制 | 化学反应控制 | |||
---|---|---|---|---|---|---|
k1/min-1 | R2 | km/min-1 | R2 | kr/min-1 | R2 | |
343 | 0.00196 | 0.9846 | 0.000209 | 0.9421 | 0.00088 | 0.9921 |
348 | 0.00218 | 0.9671 | 0.000302 | 0.9920 | 0.00107 | 0.9872 |
353 | 0.00259 | 0.9771 | 0.000476 | 0.9773 | 0.00139 | 0.9966 |
358 | 0.00285 | 0.9356 | 0.000677 | 0.9954 | 0.00169 | 0.9921 |
363 | 0.00282 | 0.9648 | 0.000779 | 0.9824 | 0.00192 | 0.9973 |
表3 不同速控步骤拟合结果R2值对比
Table 3 Contrast of R2 of different kinetic equation
温度/K | 液膜扩散控制 | 产物脱落扩散控制 | 化学反应控制 | |||
---|---|---|---|---|---|---|
k1/min-1 | R2 | km/min-1 | R2 | kr/min-1 | R2 | |
343 | 0.00196 | 0.9846 | 0.000209 | 0.9421 | 0.00088 | 0.9921 |
348 | 0.00218 | 0.9671 | 0.000302 | 0.9920 | 0.00107 | 0.9872 |
353 | 0.00259 | 0.9771 | 0.000476 | 0.9773 | 0.00139 | 0.9966 |
358 | 0.00285 | 0.9356 | 0.000677 | 0.9954 | 0.00169 | 0.9921 |
363 | 0.00282 | 0.9648 | 0.000779 | 0.9824 | 0.00192 | 0.9973 |
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